I have a question about jogging with KmotionCNC. I started bench testing a new motor this afternoon, and while everything seems to be going well, I can't seem to jog the motor and have it just stop. Basically what happens is that after the jog it will reverse direction some small amount. I can't find any reference to this behavior in the documentation, and I'm just wondering if anyone knows of there is a setting that I am missing here.
↧